深部突出矿井采空区瓦斯地面井高效抽采技术

Efficient gas extraction technology via surface wells in goaf areas of deep outburst-prone coal mines

  • 摘要: 深部突出矿井的复杂地质条件对地面井瓦斯抽采的稳定性和效率提出严峻挑战。目前地面井普遍采用固定负压抽采采空区瓦斯,在工作面回采期间,采空区“三带”处于动态演化过程,导致抽采后期效率衰减明显。以河南平宝煤业有限公司首山一矿12100采煤工作面为工程背景,提出了一种深部突出矿井采空区瓦斯地面井高效抽采技术。针对采动岩层移动对井身结构的影响,采用三开定向井身结构,优化三开钻井直径参数匹配套管,提升井筒抗地层剪切破坏的能力,确保地面井在复杂地质条件下的稳定性;结合“O”形圈裂隙分布理论、瓦斯渗流分布数值模拟与“三带”分布理论计算,将地面井布置在距高抽巷20 m处,地面井终孔布置在距回采工作面顶板上方30 m断裂带内,保障瓦斯抽采高效性;地面井瓦斯抽采系统通过抗沉降架空管路、防爆防回火安全防护、抽采监测调控等实现瓦斯稳定、高效、安全抽采;依据工作面推过地面井的不同距离,动态调整抽采负压,实现抽采效率最大化。现场应用结果表明:地面井抽采10 d后瓦斯体积分数从48%升至100%,日抽采量超10 000 m3,稳定抽采阶段持续120 d,260 d累计抽采瓦斯超235万m3;地面井抽采未干扰高抽巷正常运行;工作面上隅角瓦斯体积分数从0.50%降至0.41%,降幅达18%,地面井瓦斯抽采有效缓解了工作面上隅角瓦斯积聚问题。

     

    Abstract: The complex geological conditions of deep outburst-prone coal mines pose severe challenges to the stability and efficiency of gas extraction via surface wells. Currently, fixed negative pressure extraction is commonly used to extract gas from goaf areas through surface wells. During the retreat of the working face, the "three zones" in the goaf area undergo dynamic evolution, resulting in a significant decline in extraction efficiency in the later stages of extraction. Taking the 12100 coal mining face of Shoushan No.1 Mine of Henan Pingbao Coal Industry Co., Ltd. as the engineering background, an efficient gas extraction technology via surface wells in goaf areas of deep outburst-prone coal mines was proposed. Regarding the impact of mining-induced strata movement on the well structure, a three-stage directional well structure was adopted, optimizing the three-stage drill sections to match the casing, enhancing the well’s resistance to strata shear damage, and ensuring the stability of surface wells under complex geological conditions. Combining the "O"-shaped fracture distribution theory, numerical simulation of gas seepage distribution, and the calculation of the "three zones" distribution theory, surface wells were arranged 20 m away from the high-extraction roadway, with the well end located within a 30 m fracture zone above the roof of the working face, ensuring high efficiency of gas extraction. The gas extraction system of the surface wells achieved stable, efficient, and safe gas extraction through subsidence-resistant overhead pipelines, explosion-proof and backfire prevention measures, and regulation and monitoring of extraction operations. Based on different distances of the working face advancing past the surface wells, the negative extraction pressure was dynamically adjusted to maximize extraction efficiency. Field application results showed that after 10 days of surface well extraction, the gas volume fraction increased from 48% to 100%, with a daily extraction volume exceeding 10 000 m3. The stable extraction stage lasted for 120 days, and the cumulative extraction volume over 260 days exceeded 2.35 million m3. Surface well extraction did not interfere with the normal operation of the high-extraction roadway. The gas volume fraction at the upper corner of the working face decreased from 0.50% to 0.41%, a reduction of 18%, indicating that surface well gas extraction effectively alleviated gas accumulation in the upper corner of the working face.

     

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